The first trial with full throttle was successfull. For about 30 seconds I switched on the motor mounted in the Swing Connect Reverse harness. The thrust is about 10kg as expected, an exact measurement will be done later.
But I have to modified the electronic box. Right now the control (an Arduino Uno board) is placed in an experimental plastic case. The wiring has to be more robust to prevent the cables to get loose.
In the next days I expect the new components and switches.
I will also replace the 9V battery as power source for the Arduino board with a BEC connected to one of the main batteries.
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